 |
FROM PRACTICE TO PRACTICE: Landing Gear of modern aircraft
31.08.2009

Industry: Aircraft
Component: Landing gear
Material: 1.2083 ( X42 Cr 13 )
Machine: Droop & Rein TF + FOGS
Job title:
Implementation of efficient milling strategies for 3-D-milling in batch production towards process-optimization
- reduction of cycletime
- process reliability
- multiple machine operation
-
- minimizing of retouching work
- avoiding of customized tooling
-
- reduction of tool varieties: cutter bodies, tool holders, cutting materials
-
- no usage of coolant lubricants
- reduction of downtime
Used tooling

beforehand
- 11 different one's, partly customized milling cutters and tool holders
- stockkeeping, replacement time, replacement costs
-
- limited capability for plunging, starting drill-holes necessary, increased machining time, no multiple machine operation possible
- there is no process-reliability through increased dephts of cut, and reduced manpower is impossible
-
- program-designs are very time-consuming
-
- residual stock is to big for pre-finishing process
afterwards
- 5 tools only, Pokolm-standard tooling
- from stock, short replacement time
- all tools capable for plunging, no starting drill-holes necessary
- usage of only 2 different cutting materials
- near net-shape machining, conversion to multiple machine operation
- programming standardized
- retouching work cut in half
- change-over from drilling to helical milling, no coolant lubricants
Example from practice
|
|
| |
 |
 |
| |
|
|
| machining: |
roughing |
finishing |
| tool: |
5 52 300/7 (diam. 52/R8) |
35 201
(diam.35/R8)
|
| inserts: |
04 16 844, P40 |
04 16 835, HSC05 |
| coating: |
PVML |
PVTI |
| arbor: |
100 22 710 (diam. 22/SK50) |
75 16 A63 (M16/HSK 63 A) |
| vf (feed rate): |
5000 mm/min
|
15000 mm/min |
| n (revulotions): |
1200 1/min
|
12000 1/min
|
| ap (cutting depht): |
2 mm |
0,5 mm
|
| ae (cutting width): |
40 mm |
1,5 mm
|
| chipvolume: |
400 cm³/min |
- - -
|
| |
air through spindle |
air through spindle |
| tool life: |
2 hours
|
20 hours
|
| |
|
| Result:
The total machining time has been reduced from 110 h to 60 h!

Do you want to reduce your costs for machining times too? Use our consulting capacity and get in contact with us!
Print page
|
|
SEARCH
LANGUAGE
QUICK NAVIGATION
|